Everything posted by Patcon
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Chat GPT - AI Bot
@Mike There is an error on the forum now. I can't click my user profile or anyone else's and see their stats and activity streams Charles
- Duffy's 1/71 Series 1 240z build
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Still struggling with car at idle after 8 years
I agree with Zed. Numbers are way low. Bad gauge, bad methodology or bad rings... Updated signature would help the memory Multispark would be interesting maybe Megajolt? Although tuning could be an issue... I would want something as hot as I could get. Blow your fingers off hot! 😉
- Duffy's 1/71 Series 1 240z build
- Duffy's 1/71 Series 1 240z build
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Still struggling with car at idle after 8 years
Very low unless those are not in PSI. Plugs 5&6 seem a little lean. I know we have gone through the ignition system before but don't remember everything that was tried. An all new hotter ignition system might be worth a try before you dig into the motor
- Duffy's 1/71 Series 1 240z build
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Still struggling with car at idle after 8 years
But oil ring shouldn't affect compression numbers
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71 Vapor Tank Hoses
I believe he is referring to the extra metal in the passenger side wheel well Zcardepot offers this piece
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71 Vapor Tank Hoses
$277.77 All 10' lengths in 2023
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Steering column lower u-joint replacement part
Im sure I documented that somewhere on the forum but I can't find it. I thought it was in my build thread but maybe not. Maybe the librarian can find it? As I recall the shoulders of the spider were too wide to tip into the yoke. So they had to be shaped down to fit in
- 71 Vapor Tank Hoses
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1971 HLS30-14938 "Lily" build
@Namerow Now you tell me 😉
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Still struggling with car at idle after 8 years
But it doesn't make sense that only #4 does it and not 5&6. We also went throught ignition trying to move it and couldn't
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AC fuse keeps blowing
I think Zeds right look for a pinched wire in the dash
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Still struggling with car at idle after 8 years
I believe he stated earlier that the valve seals on #4 had been replaced
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1971 HLS30-14938 "Lily" build
I'm confident it was put on before the plugs when new. Just makes replacement challenging
- 1976 280Z Restoration Project
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Steering column lower u-joint replacement part
Yes, I used that part. It can be a little tricky to reassemble. I had to clearance the one I got some. Not every needs to though.
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Upsize tire options for Z32 with stock wheels
I don't mind the stock wheels. They look right to me...
- 1971 HLS30-14938 "Lily" build
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1971 HLS30-14938 "Lily" build
I did a little work on the car today. Finished assembling the rejuvenated clutch master. I also worked on the engine bay harness. I laid new wires into it and replace the firewall grommet. What a pain in the ...!!! You have to depin most of this to get it on. And some of those wires don't want to depin, even with the correct tools. I did finally get it. Hopefully I got them all back in the right spots. Otherwise SteveJ is gonna have a fit finding it!
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Upsize tire options for Z32 with stock wheels
Pretty car. Looks to be in pretty good condition.
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1976 280Z Restoration Project
We have a crank shop near us that regularly reworks journals like that. They weld them up and then remachine them. Probably not cost effective. Especially if the offset grind L28 will accomplish almost the same thing. Hate it about the motor, but the new engine aught to be impressive
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Still struggling with car at idle after 8 years
True but we never got it to move from cylinder #4 no matter what we tried. Maybe the oil ring is bad or the gaps in the compression rings aren't properly offset. Ive got no idea but there must be some cause and it seems like we tried everything else