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Captain Obvious

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Everything posted by Captain Obvious

  1. No kidding! Looks great!
  2. Captain Obvious posted a post in a topic in Introductions
    Where did you get the steering wheel? And, I hate to ask, but... How much? @charliekwin
  3. Captain Obvious posted a post in a topic in RACING
    Hahaha!! Kim Cardassian! That's awesome!!
  4. Haha!! Exactly. "And then a completely unprofitable huge amount of time later, you have this...."
  5. Well any more evaluation will have to wait until the rains stop, which at current forecast may be.... Never?
  6. Keep me posted as to any of these plans as well!!
  7. One of my off season projects for this year was to replace my sketchy looking intake duct tube between the AFM and the throttle body. I couldn't see any cracks all the way through, but it's just a matter of time. I know there are aftermarket repros available, but I've always kept my eyes open for other cars that had air intake tract hoses that looked similar to the 280Z. With that in mind, and my never ending quest to find cheap ubiquitous replacements for OEM parts, I nabbed this on off a 2002 Ford Taurus: Here it is compared to the stock connector. The angle is almost perfect, but there are some issues. First, it's a little too long and second, the big end (AFM end) is too big: Taking care of the length is simple. Quick work with the razor knife to remove about a half inch from the small end where the hose clamp was and then put the hose clamp back on a little further up: Second problem... The big end is a little too big. The AFM is 2.75 diameter, but the Taurus hose is 3" diameter: So I made a spacer ring out of aluminum: Put a little sealer on the joint and press the spacer into place. Now I've got an AFM with a 3 inch outlet instead of the original 2 3/4 inches: Put everything back on the car and it looks like this. Cheap, ubiquitous, and although it isn't stock, it doesn't stand out like blue silicone tubes. One more step in having every molecule of air going through the AFM instead of around it: And now that I've got the projects mostly done and have a couple miles on the car, I was able to take about a half more turn out of my idle mixture screw. The car used to like it at about 4 1/2 turns out, and now it likes it about 5 turns out. So between my tight sealing Delrin bushings on the throttle body (this thread here >>http://www.classiczcars.com/topic/57126-sticky-throttle-body-fix-delrin-bushings/), and the new intake tract duct, it seems I've got a little more air going through the AFM:
  8. Thanks guys! That pinch bolt is pretty tight, and I really doubt that it'll slip, but you're right that it could happen. I'll keep my eyes on it. I can just reach the strap with a couple fingers with the car on the ground. That way I can check tightness without jacking anything up and crawling underneath. Makes it easy to tell without much difficulty if anything has loosened up. I'll keep you posted!
  9. Captain Obvious posted a post in a topic in Engine & Drivetrain
    Love the AC/DC shirt. Ride On.
  10. Nice work. Have the orders started coming in yet?
  11. Haha!! That was the emergency meeting. That's the one we had to call Cliff to let him know. Funny... Only had to call him once!!
  12. One of my off season projects for this year was to replace my temporary light duty nylon web diff strap with a more substantial version made using a stronger webbing which I purchased from McMaster. I also figured out a simple way to adjust the webbing tension to account for stretch that may occur over time. Here's what I started with. The blue webbing is whatever the local hardware store had on shelf. Worked great for the six months it was on the car, but I had already planned on replacing it after proof of concept. The black webbing is McMaster P/N 3510T83 - Shock-Absorbing Nylon Webbing, 1-1/2" Web Width, 5100 lb Breaking Strength: To adjust the strap tension, I designed a new adjustable anchor bracket for the driver's side mount. I had originally planned to put these new brackets on both sides, but the diff doesn't sit in the middle of the tunnel, and it was an uncomfortably tight fit on the passenger side. With the help of our resident sheet metal magician @disepyon doing the bending for me, here's what I came up with: Here's the adjustable anchor assembled. The strap loop goes around the center shaft and the bolt slides in the slots to adjust: Here's my new strap in place. Original anchor on the left in the pic my new anchor on the right in the pic (driver's side): And here's my adjustable anchor bracket in use. Loosen the bolt, pull down until desired tension is achieved, and then tighten the lock bolt through the middle: Works great!! Thanks again disepyon for the help!!
  13. Looks great so far. I'm assuming the stitch design will make more sense to me when it's done.
  14. I'm so there!! I'm getting to Austin on Wednesday mid-day or so. Hoping to grab the rental car and head straight to the Oasis from the airport. I've got a local place to stay, so I won't have a room at the host hotel, but I'll be there for the CZCC meetings.
  15. He turned me into a newt.
  16. Captain Obvious posted a post in a topic in Open Chit Chat
    RIP Greg and Chris. I was out at a bar last night and the entire time they were playing Chris Cornell in all different configurations. I was very pleased with the music choice.
  17. I agree completely. I'm positive he weighs the same as a duck.
  18. "Or I could buy a stitching awl and do it all by hand." I unfortunately believe this would yield the best results.
  19. Arrrrrgggh!!!
  20. I would use a cheap generic relay with maybe a 20A rating, and put it in an accessible spot so that when the contacts burn up, you can just pull it out and replace it with a new one. I don't think I would go as far as to use a 40A continuous rated relay.
  21. That's exactly what I answered. 30-40A for an instant, and then about 8A continuous after that until you release the key.
  22. I have. First, let me point out that the starter solenoid actually has two coils inside it, which are wired in parallel (a "pull-in" and a "hold" coil). When you first apply power to the solenoid, both coils are activated and are used to PULL-IN the solenoid. Once the solenoid has pulled in, one of the coils is disabled and just the second coil alone is used to HOLD the solenoid in place. So the answer to your question, based on my measurements is... When you first apply power to the solenoid, the solenoid current will very quickly ramp up to between 30 and 40A for a short period of time until the solenoid has pulled in. Then once the solenoid has pulled in and disabled one of the internal coils, the current will drop to about 8A when just the "hold" coil is energized. And by the way... It's those high currents involved that eats ignition switches for lunch. Here's a guy who took apart a Bosch starter solenoid and talks about the two different coils: http://www.ifitjams.com/solenoid.htm
  23. Captain Obvious posted a post in a topic in Help Me !!
    Haha!! I wouldn't eat those...
  24. Captain Obvious posted a post in a topic in Help Me !!
    And if you get stuck, send me a PM and I might be able to swing by to lend a hand.
  25. Haha! That's exactly how most of my projects go: "And then a completely unprofitable huge amount of time later, I have this...."

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