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240Z reproduction calipers?
I can't imagine they'd be cheaper than $33 (or still even $44 if I send in my cores).
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Michaelwk started following 240Z reproduction calipers?
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240Z reproduction calipers?
@foosman Checking in to see if you installed these. Any issues? Looking at them as well.
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So we're doing a 73 restoration project
I will probably ask about that. It's an insulated but not heated section of a big shop. There's a good number of other cars, bikes, and boats stuffed in there so we'll have to see how much room there is.
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So we're doing a 73 restoration project
Hi jayhawk, I was going off the FSM for 73, which shows this picture: That bowl has 6 screws and nice little easy-to-remove setup for the float. I most certainly do not have that! haha. I agree with you that I have the -2 that the Fuel Modification doc talks about, so it's odd that the 73 FSM doesn't talk about these. Unless there's two versions of it out there. Thanks for the info!
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So we're doing a 73 restoration project
Well, as I tried to drive it off to storage today, I had the same fuel issue. It actually fired right up but then died about 2 minutes later. I found that the fuel filter, which was replaced when I started this work, had caught a fair amount of crud. I didn't notice much, if any, before I drove it Sunday, and that day was probably 15-20 minutes of idling and 20 minutes of driving. I blew some air back into the tank and that did the trick. Started up and ran fine. Would it be a bad idea to drive it again? The storage place is ~20 minutes away. If I do clog it again, I can always do the same thing again I assume. And obviously first thing to do in spring is drop the tank and get it properly cleaned.
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So we're doing a 73 restoration project
Absolutely! I'm so bummed that it took me until December to get to this point, but glad it's moving. And thanks a lot Captain for all your help!
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So we're doing a 73 restoration project
Ok, sorry again for the long delay between updates. I haven't had much time the past few weeks with Thanksgiving and some traveling for work. But good news, I took the Z on it's first drive since 06 yesterday! There was indeed one major vacuum leak in the braided, curved hose going from the anti-backfire valve to the manifold. I found a hose at Autozone that worked, although it was not metric, so it's a bit oversized and it wasn't quite the same curve, so it's running over the top of stuff instead of under. Will try to find a proper replacement later. I'm guessing some the other hoses are not completely air-tight at the connections. I did try to address that with some zip ties and hose clamps, but again, I just need new hoses. Will address that next spring. Yeah, I see where you're looking. It's actually just really thick parting line flash on that hose. I also continued to have problems getting it started, even with the new coiled. Turned out this was fuel. For some reason the new mechanical pump cannot pull anything from the tank without priming. Took me a while to figure this out, which was frustrating, but once it's primed, it runs pretty well. I stopped and started it several times and it fired right up once warm. I'm going to start it again tonight and see if that is still a problem. If so, I'll definitely be swapping in the electric pump first thing next spring. I never did the compression test again, will save that for spring as well. Getting up to temp definitely made things better. The idle wasn't great, so I have the idle screwed turned in one turn. I drove it around the block and then to the gas station to put some fuel in. Was so much fun to drive (even at only 35 mph), I'm sad that it's going right into storage. But really was fun to cruise around a little bit (even with the window down in 25 degree weather)
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So we're doing a 73 restoration project
I realized I had the choke closed when I did the compression test, which was incorrect. The directions said have the choke open, and to me that meant "engage the lever", which obviously is wrong and doesn't match what the throttle plate is doing. So that was probably the issue. I attempted to repeat the test this past weekend but couldn't get the engine started. After cranking a while the battery died. Using my other car to jump still didn't get it to fire. Back when the car was driving, it always needed a lot of cranking to fire, my dad attributed this to the electric fuel pump being shot, but I also read that this could be due to a bad coil. The coil looked like the it was still the original, so definitely time to replace anyway. I attempted some trouble shooting prior to replacement but wasn't quite sure if what I was getting was correct. At key-on, there was ~5V at the coil. Everything I read said this should be 12V. But the new coil is giving ~5V too, so I'm now assuming that's correct. I also replaced the plug wires while I was at it. I thought about doing the points, condenser, and distributor cap too, but that actually looked really clean. I am guessing it was replaced in 03/04. Got the new coil in tonight (with temporary cardboard spacer). Anyone have a recommendation on a different bracket or proper spacer to use? Battery was all charged up and it still took a good amount of cranking to fire, but it did eventually go and seemed to run better than before, so I'm pretty happy. I let it idle with the choke on (closed!) for a while and was able to drop it to about half to 2/3 open eventually, but it still ran a little rough. The temp gauged climbed a bit high so I shut it off. I need to top off the coolant before a test drive. So, took a step backward and didn't make any progress on getting it to idle better. Thanks for advice on looking for vacuum leaks @Captain Obvious, I will try to tackle that this weekend. I don't get much time during the week to work which stinks. It's getting cold in Wisconsin and my winter storage location might give away my spot soon! Michael
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So we're doing a 73 restoration project
I just finished the compression test. Uff da. We've got 130, 130, 132, 140, 120, and an even 100. I was not moving super fast, so the last couple could be just because the engine was cooling down, but not even getting to 150 on the first few was unfortunate. Wet compression test improved them all, so I'm concluding the rings are just pretty worn. The engine also couldn't idle. It only ran when the choke >50% open. I wonder if this is part of the reason the floats were set so high. Would running it rich make up for poor compression? My dad had a local mechanic get the car running back in 2003 and doesn't know exactly what he did. I'm guessing the compression wasn't great back then either since we didn't put many miles on it back then. It's also seems to have all the original hoses so I there could definitely be vacuum leaks. Will try to diagnose that this weekend and see if I can get it idling and possibly even take her for a test drive. Short video of the car running. The white smoke went away after it got up to temp. The throttle was also stuck during this video which is why it didn't die when I pushed the choke down. 20181108_181910.mp4
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So we're doing a 73 restoration project
Thanks for the advice on the new pin. I didn't get a chance to take the pin and screw into work, but I think we should have some metric rod stock to use.
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So we're doing a 73 restoration project
Alright, another positive update. Managed to get the second float pin out today, cleaned up the dirty parts of the second carb and replaced the power valve gaskets and needle valve. Got my replacement rebuild kit on Friday but another disappointing find regarding it, the float cover gasket swells after coming into contact with fuel... so trying to reuse it is a PITA. Was able to get it back into the groove once, but couldn't the second time. Just reused the original gasket. I doubt you can buy those outside of the kit, so we'll just hope the old gasket still works for now. Adjusted the tangs on the floats to get the fuel level into the middle of the window and meet the dimensions from the FSM. I was surprised how far off they were from the recommended dimensions. I wonder if the floats were replaced before and just half-arse adjusted. Managed to get the carbs back on the engine, even with the one busted hose. Just stretched it a bit to reach. Anybody have a good source for random hoses? The specific one I need is the air bypass hose that runs between the two carbs. Has a couple sharp bends, so I don't know that a regular straight hose would work. After getting the air cleaner back on, I gave her some choke and it fired up! Checked quick and no oil or fuel leaks were immediately present and the oil pressure was right in the middle of the gauge. Tried to put the choke down a little and it died. Started up again and saw there was a good bit of white smoke coming out the tail pipe. The engine also sounded a bit louder than I thought it should so I turned it off. Next up I think I'm going to do a compression test and see how things are looking. Did not get a chance to try and see the fuel level with a mirror while the car was running but that's ok, not looking to do any fine tunes right now. Just happy that it finally ran.
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So we're doing a 73 restoration project
Good news! Letting that pin sit in some carb cleaner long enough got it loose. Got the utility knife blade in there next to the float like you mentioned @Captain Obvious and was able to push it out and grab it with the tweezers. I like your new float pins! I've got a machine shop at work, maybe I can talk one of the guys into making me a couple new pins and modifying the cap like yours. Started on the second carb tonight as well. Again the pin is quite stuck. Will give it a few rounds of carb cleaner and try again in a few days. Comparison pic of the old valve seat (left) and new one from the rebuild kit. The pic doesn't show the exact height of the valve as they were a little closed, but the new one does seem a bit longer. Will have to adjust that tang on the float maybe. Going to wait until I have both carbs ready and then redo the fuel level measurements.
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So we're doing a 73 restoration project
Yeah, I was thinking of using heat as well. That Rusty nut remover that was linked previously might be a good choice. I think I'll stay away from torches with fuel in the vicinity. Probably have to keep the heat away from the floats though... don't want those to soften and warp. Could be tricky... I did try the razor blade as well with no success. Will think on this one for a while. Ruining the float will be the last resort.
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So we're doing a 73 restoration project
Alright, I finally got chance to work on the carbs today. Tried to pull out the float pin with a tweezers but no luck. That sucker is in there tight. Let it soak in some carb cleaner few times and still nothing. Took apart the power valve and cleaned that as well. Realized one of the two rebuild kits I got from rockauto didn’t have the valve diaphragm I needed… not a huge deal since the other kit did have it, and I only got through the front carb today. But I did freak out a bit thinking I had the wrong kit somehow. I gave the fuel window a good cleaning too from the outside. I would have liked to clean the inside too but the float bowl is in the way. After reassembling and filling it up, it actually looks like the fuel is at the top of the window, rather than in the center. I am assuming the carbs sits perfecting level in the car, right? If it was tilted toward the rear of the engine bit, the fuel level would be better. Looking at the car it was hard to tell as it is on jacks and not perfectly level. Assuming the level is too high, could this be a worn needle valve? Or sunk float? I’m thinking maybe just tear out the float and buy a new one. That would allow me to get a pliers around that pin and push it out. New float bowl is only $30 on ebay.
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So we're doing a 73 restoration project
Interesting tool... that might have to be a christmas present to myself!