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madkaw

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Everything posted by madkaw

  1. Might look at the first page of the Triple Mikuni Thread. I made the linkage piece between the firewall and the carbs. Either I got lucky or made it right, but it's been flawless. Real good pedal feel and never hangs up, better than stock SU's. I feel your pain with those annoying items that take away from the ride!
  2. No, I never did try this. It seems all that I have read says 400-500 for 4 or 5 hours. I was also considering a powder coating shop for the job. Need to make a hefty fixture to bolt down the head to. My head is probably. 030 out, so it would take good size shims. I came across 2 more good heads so there was no need to rush into this fix. I'm going to use my warped mn47 for the flow bench so it doesn't matter much
  3. Last time I mentioned here ,the fact I was going to straighten a head ,it was considered crazy talk. The fact is there is few shops that will do this. Usually just told to find another head. Bolt it down with some shims and throw it in the oven with the chicken dinner and see how it comes out. Cook it low and slow though!
  4. I never had a problem with the first one. Just a dumb design that could be prone to problems .
  5. You need to look at the possibility that the head gasket has been compromised by overheating . So now your temps are steady when running? Might borrow or use a pressure tester that mounts on the radiator. Put it on and run the car and see if pressure rises too high. Start pulling spark plug wires while pressure is rising and see if pressure drops.
  6. Bought this little gem because I thought the idea was good to see when things got dirty. It left me stranded on the road at 11pm on the way to work. Had to leave my Z in a church parking lot until towed to a buddies house. I had previous issues with my engine acting like it ran out of fuel, but blamed my Mikuni's and my Holley regulator. You could see fuel in the glass so I ASSumed all was good. after it left me stranded me and my buddies dug into things and found that the fuel flow stopped at the BRAND NEW filter. The cartridge filter is held inplace on a threaded pipe by a nut. I guess they didn't get it tight during assembly and the nut was free to rome up and down the threads. It eventually loosened up all the way to one end which then CLOSED off the only entry holes for incoming fuel. BAD DESIGN-period. I called Mr Gasket and let them know. Might be different if I had assembled it or the instructions said to check tightness, but it did not. I threw the SOB away and bought a 5$ plastic one. signed P.O.d
  7. Do it, that's close to me and would love to see it!!
  8. Datsun reliability wins!! Not sure how a 944 that does 9mph more on the straight away is even in the same class. Way to hang in there Greg . Nice way to retire from EP!
  9. Cliff, I think you are being a little paranoid, but I understand. I think cold specs will be fine for break in. After your initial set up and run check them hot . My conversations with Schneider I was told that the 20 minute break in at 2000 didn't apply to our valve train- just saying what I was told. Did I do 20 minutes, not exactly . Definetly not 20 at 2000. Didn't do it on either of my Schneider or Isky cam. The issues I experienced were with improper valve guide install, but the wear on cam lobes looked perfect. Just think about how many folks have everything dialed in so well on a total rebuild that it just fires up and runs for 20 minutes no issues to deal with. It seems to me that a lot of cam issues are from not making sure the system is primed well enough for instant oil on the cam with start up. Prime the motor with a drill and watch the oil bleed out on to your can before you ever start the motor. A slight valve clearance issue will not hurt anything.
  10. I guess when I considered an answer I should have remembered that I was using light springs, so wear wasn't a concern. My machinist just used permanent marker with light springs. Probably with full on springs a little lube wod be good.
  11. I don't see why you need to grease if it is spotlessly clean!
  12. Look at my MS3X install thread on Hybridz or the thread I did hear .
  13. So did you loosen the crank pulley bolt back up and tried to turn the pulley to see if turns(key gone). I think I would want to see ALL of the bolt too, to make sure it didn't break in half. That Murphy guy sure has a sense of humor-
  14. Wow, what a challenge. Sucked that it made your race day short-crapcan race? Loose damper could lead to sheared keys .
  15. So have you verified that at TDC #1- compression stroke- that the dizzy shaft is at the proper 11:25 position and that the rotor is lined up with 1 plug? Please understand with any posts regarding shiny links is irrelevant UNLESS you have the timing cover off to see the crank sprocket. What ignition issues were you having prior to this?
  16. Looks like about the same specs as the Carter. Is it quiet? I also went with the carter because it is in line and will package well for my tight space.
  17. Well it wasn't terrible, but the pressure wasn't stable. At WOT pressure dropped to 2psi. Pressure was also shaky in transitional areas. Upon looking at the numbers on my fuel pump I realized that I had installed (and recommended-sorry) a pump that probably is slightly to small in volume. The rx7 pump was made for a 1.2 liter rotary and requires only 15 gph(2-4psi) Maybe sufficient for a stock Z with SU'S , but not enough for my engine. I have ordered a Carter p60504 to replace my pump. It's rated 4psi at 30 gph. Reading Racetep ' s page they run Carters with 4psi and no regulator on all there set ups. Waiting on the pump and leaving the pressure gauge in place to see the changes. I will say that after adjusting my Holley regulator up right to 4 psi the car ran really well- EXCEPT it stumbles in transition sometimes and I can watch the wideband go lean. I'm thinking -hoping - the increased flow with help keep float levels at optimum level to combat my lean issue. We will see
  18. Sorry to hear the news. Glad no one was hurt.
  19. Wow, so many different ways to do one task. Been all over looking at triple fuel line routing and it's hard to compare anything. Racetep recommends Carter fuel pump and No regulator. Some run regulator to deadhead, some regulator with return . Some say you have to have a return, others say no. Then you throw in the variable that everyone's car runs perfect on their set up (whether it does or doesnt). Other variables like what pump they are using . I think there is something to be said that most FI use a regulator after the injectors and use a return. I think that's the route I'm going .
  20. 99.99% sure it's fuel. haven't pulled the plugs but I'm pretty sure what I will find. I'm running my MS which turns the pump on and off. Not sure why it got so bad so there is much to check, but had to walk away for while.
  21. Running an rx7 pump and it's quiet. Changed whole system over to a Mr Gasket regulator (non bypass), and car ran no different. In fact , on the way home it kept acting like it was running out of gas- almost didn't make it home. So I like your thinking Ryan. Stopping fuel flow to 3 carbs sounds like it wouldn't keep up with volume. Even today the car ran great WOT, but transition, idle was crap. So build up of pressure would happen at low demands so causing this type of regulator to shut off fuel. High demands at WOT the regulator just opens up. Is this what your saying? Lots to think about and research. Might need something better than a 40$ regulator.or maybe run a return
  22. Interesting. I guess that will be suspect as well as everything else. It's interesting that my gauge will show 3 psi at the regulator after it stalls out from running out of gas.
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