Well it's like watching one of those car shows where all kinds of things happen at the last minute. So I lost a day and half because Isky put the wrong numbers down on their cam. Things roll pretty good installing the motor, but not sure I will install a motor again with all the carbs on. It throws the balance off longitudinally , so it makes it tough lining things up. The trans was a bit tough lining up, but the old man squeezed her on.
So pour coolant in the radiator and watch it drip out of my thermostat housing. turns out the housing is cracked
Not a big deal EXCEPT, Mikuni shorty intake means it all has to come off to get the bolts on the housing -SH!T. So that added an extra 3 hours of work. Went thru diagnostics last night and the fuel pump didn't work. Tested wires and ended up at my inertia switch-just needed to be reset!
Fired off the coils and they tested okay. So I'm ready to start it this morning and the battery is dead. Some dumb arse left the ignition on all night.