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Phred

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Everything posted by Phred

  1. :stupid: Sorry to rag on this, but your duration numbers are bogus. Also the 262/272 numbers are useless without reference to int. or exh. and at what lift were these numbers taken? Advertised, or actual timing figures? Different cam grinders will sometimes specify special lift numbers to degree a cam, and then advertise it with theoretical duration numbers. So, whenever you quote cam specs, be sure to get the whole story, or it just adds to the confusion. The only way to compare cams is to note the lift (usually .050) at which the duration points were taken. The theoretical, or complete duration looks good on paper, but is not usefull. Because of the lash used in a running engine, the duration numbers (the amount of time/distance measured in degrees) will not be representative of the advertised numbers unless the cam is degreed with the lash specified by the cam grinder. Yes, it can be confusing. Just be aware of the facts, and don't throw out numbers without all the specifics to back it up. Phred
  2. Phred replied to broken74's post in a topic in Engine & Drivetrain
    Factory Service Manual Specs: 4.5 to 6.5 ft. lbs. I assemble these frequently and use a in. lb. torque wrench set at 72 in.lbs. Over torque can split the gasket at the bolt hole. Phred
  3. I agree with Bambikiller. Also don't waste your money on the Nissan Comp. race damper. Its very expensive, and you dont need it unless its an all out race engine. The euro damper only has one integral pulley groove. If its a street car just a standard replacement damper will work fine. Since it came loose, the front seal may also need replacing. Check the threads closely on the attaching bolt, and replace it if damaged. Reassemble it with locktite and 95 ft./lbs. torque. Phred
  4. Phred replied to san_maru_zed's post in a topic in Engine & Drivetrain
    You'r close Walter, L-28 cranks are from 46 to 48 lbs. Phred
  5. Xtinc, The gap between the plunger and body of the tensioner on your engine is not unusual if it has had the deck surfaces machined. To determine how much the head has been cut is easy. A stock L-series head is 4.250 thick, ( from cyl. deck to cam deck.) You must use a digital caliper or micrometer to measure it, then you'll know how much its been cut. Its harder to measure the block height when its assembled, and I can't remember off the top of my head how tall the stock block is anyway. Be carefull when (if) installing cam tower shims on an engine which has a used cam and rockers in it. The cam/rocker contact patch will change, and will require different thickness lash pads to realign the contact area. If you have the same cam/rockers as were used prior to your rebuild, and they are both stock, I would run it as is. The only other very minor consequence will be a slight increase in the wear on the bottom of the tensioner rubber, as the chain won't run smoothly againt the face of the rubber for the first few hundred miles. This will not degrade performance or engine life. The only other problem I see from your picture is I don't see any washers under the heads of those bolts holding the tensioner or chain guides. Washers are important here, as they distribute the tporque load. Its not unusual to find broken chain guides in improperly assembled engines. Use a flat and a new lock washer on these parts, or just a flat washer with locktite and 7 ft. lbs. (or 84 in. lbs.) of torque.
  6. halz, good point to consider! Some race shops will use a +/- .5 ( one half a cc) as a maximun deviation. Which means if all six chambers are within one cc, its good to go. This is usually acceptable, untill compression ratios start to get critical, (12:1 & up) and total compressed volume gets small. Then variance between chambers should be kept to +/- 2 or 3 tenths of a cc, Also, use the smallest chamber to compute compression ratio. It may be helpfull to try this formula for computing compression. Its quicker and less involved than others. First, compute displacement of one cylinder bore x bore x stroke x 16.387 x .7854 Then compute total compressed volume: vol. of one chamber + vol. of head gasket + vol. above piston at TDC ( example- a dished piston, or if a flat top piston is below the deck at TDC) To find compression ratio: Divide displacement by total volume and add (1) Phred
  7. Attn. jmortensen, Your on the right track. A few little tricks will ease the effort required to cc your head. Install the spark plug with a little white grease on the threads, also dab a little of the same stuff on the valve seat area, and then drop the valve onto its seat. The white grease is easy to see and will seal the chamber, no spring is required to hold the valve down. Then seal the plate over the chamber with the same white grease, again because it is highly visible, and creates a good seal that won't wash away, but can be wipped off easily. Then, drill the hole in the plate offset so it is located at the edge of the chamber between the valves. Then set the head up on your bench at a slight angle so the hole is the highest point. Then when filling the chamber, the air will escape out the top leaving no bubbles to contend with. Finally, use cheap rubbing alcohol (99 cents a bottle) and add a little food coloring to aid visibility. The rubbing alcohol has low surface tension, and will flow more easily than other liquids. If you're really into this sort of fun, go down to your local pharmaceutical supply house and buy a cc burett. Zero to 100 cc's works best. I've been doing this for many years, and have found this to be a fairly cheap, painless way to get accurate readings. Phred
  8. Phred posted a post in a topic in Old For Sale Ads
    Four row radiator for sale. New four row core installed in a stock 1971 Z radiator. Have invoice for $218.00- used for six months. Been in clean, protected storage since 1999. My plans have changed, and I will be using an aluminum radiator for my race car project, so this must go. $180.00 plus shipping, or pick up in Portland Oregon. Phred
  9. Cam, rockers, timimg gear, even valves, retainers, keepers, all that stuff I'll give you a few buck for if you can't get rid of it locally. Phred
  10. Proper steps to timimg happiness. First verify TDC on the compression stroke. Pull # 1 spark plug out and stick your finger over the hole. With a remote start button or with a socket on the damper bolt, turn over the eng. till it blows your finger out of the hole. Now with a light to peek down the # 1 hole, and the wrench or socket on the damper bolt, turn the engine very slightly back and forth to visually confirm the piston is at TDC. If you have trouble seeing, stick a screwdriver in the sparkplug hole as verticly as you can and then again turn the engine by hand slightly back and forth and watch the screwdriver go up and down. After you think your as close as you can get to TDC, check the timimg marks. Put a small dab of white paint on the damper pulley where it aligns with the timing pointer. Now you have located TDC on the compression stroke, Probably within a few degrees if you have a good eye. Now hook everything up, set the timimg light to ten degrees and fire it up. Final note, do not exceed 36 degrees total advance. good luck. Phred
  11. Phred replied to 240ZMan's post in a topic in Help Me !!
    That type of screw extractor tends to expand the part your trying to get out, so don't crank on it too much or you will split the bolt. But, I think you're in luck. The pic shows you have about three threads above the deck. I have removed many broken bolts with this method. Get a nut with the same thread as the head bolt. tighten down the nut all the way to the deck. Weld the nut down through the center, to the remaining bolt with a TIG welder. Then simply remove the nut/broken stud with the proper size socket. The heat from the welding process will also tend to loosen the rust bond to the block. Good luck. Phred
  12. Phred replied to mayolives's post in a topic in Engine & Drivetrain
    Ed and 2Many are correct. Because of core shift in castings, one block may be able to go .120 oversize. While another block might hit air at .120. Its best to error on the safe side, and only go .040 over, especially on a turbo where pressure and heat are greater than a N.A. engine. I have used a sonic tester on blocks, and I can assure you that there are good blocks and bad blocks. Also since you are looking for a quality job here, specify that your block be honed with a deck plate, to be certain that the rings have a nice round bore to seal up to under that extra cyl. pressure. Phred
  13. Phred commented on panchovisa's comment on a gallery image in Big Z Photo Collection
  14. Phred replied to zeiss150's post in a topic in Engine & Drivetrain
    You get an "A" Mark. Fly cutting pistons gets its name from the type of tooling, or cutter used to mill reliefs in the tops of pistons. When aftermarket cams are used that have higher lift, and longer duration, they sometimes can come in contact with the pistons. This usually happens from ten degrees before, to ten degrees after TDC. Most race engine builders will temporarily install the pistons, then set the head on with no valves. Then with a long center punch made out of an old valve, drop it down through the valve guide to make a small mark on the piston top. Then with the pistons disassembled, and mounted in a special holding fixture, the cuts are made in the pistons, centered on the marks made with the punch. Then final checked again to assure that they have the required clearence. Safe clearence for valve to pistons is generally .060 for the intake and .090 for the exhaust. This operation is sometimes referred to as Bridgeport cutting for valve to piston clearence, because a universal head Bridgeport milling machine is commonly used. Phred
  15. Phred replied to MikeT73's post in a topic in Open Discussions
    Ditto to what 2ManyZs said. I might add if you have any children you can sell, you can get more parts for your Z. Phred
  16. Phred replied to fatones's post in a topic in Engine & Drivetrain
    Hi Tim, FWIW, I built a forged piston engine for street use, a few autox, and general driving. I started it out with .005 pist./wall clr. After 54K miles I took it apart mostly cause I just wanted to see how it was doing, and for a rebuild. Every thing was fine, so I honed it and put in a new set of rings. It then had about .0055 clr. I sold it so I don't know how long it lived after that. Iv'e heard some people say forged piston engines make a little more mechanical clatter till their warm, but I couldn't say that. Consider stock cast pistons have about .0015/.0025 clr depending on where you measure them, against .005/.0055 for a forged one. .003 difference, not much. I have never used any of the hyperutectic pistons. Phred
  17. Also be aware that it is possible to have good compression and oilfouled plugs. The compression rings control compression and the oil ring controls the oil. so if you have a bad oil ring and good compression rings, it can smoke and look ugly, and still have good compression. Another possible culprit is a plugged breather system. Crankcase pressure would then seek the line of least resistance, that is, the weekest cyl. to vent into. But you will usually see leaking seals when this happens. An old engine builder once told me, The more you know doesn't make it any easier, just more confusing. Phred
  18. Phred replied to greenmonster80's post in a topic in Old Want Ads
    Greenmonster80 I am also building a stroker with the LD-28 crank, but I'm only going .040 over and should end up with 2964cc. I wanted to fit in the longest rod that was physically possible. So I called Carrillo. They had some and listed them as L-16's. But these are 140mm (5.511") long, and I thought L-16's were 133mm long. I then called JE Pistons and had pistons made to match the rod length and stroke. Look at the picture and you'll see there is no way to fit a longer rod in an eng. with the LD-28 crank. And yes, I had to rob a few piggy banks to get it all. Phred
  19. Phred posted a post in a topic in Technical Articles
    Shot Peening - A Practical Guide For The Racer The principal function of peening is to increase the fatigue life of cyclically stressed parts. Small steel balls (shot) hammer the part, compacting the surface, which relieves both surface and granular stresses. The process builds a tough outer layer which is very resistant to fatigue cracking. This protective skin actually strengthens the part. The usefull life of a properly peened part is usually two to five times that of an untreated part. Shot peening is of most benefit on con rods and crankshafts. It can also be applied to almost any part subject to fatigue cracking. The following preparation is necessary before a part is peened. 1. The part should be Magnafluxed or Zyglo inspected. 2. All sharp corners, nicks, maching flash, and similar stress risers should be removed, smothed, and properly radiused. 3. Precision finished surfaces, such as pin bores or journals, require masking prior to peening. Intensity is the critical component in successful shot peening. High intensity peening will distort a thin section part. Peening intensity must be high enough to produce an effective skin, but not so great as to damage or distort the part. Controlling intensity in the peening process is accomplished by using shot of different density and diameter. It is also controlled by the distance from the gun nozzel, angle, air pressure, and exposure time. The intensity used for different parts also varies with the type of metal being peened. The ideal intensity for a specific part is determined by knowledge of metalergy, experimentation, and experience. Double Shot Peening: Most parts benefit from double shot peening, wherein the part is first peened using larger shot and high intensity. Then peened a second time using smaller shot, (usually fresh glass beads) and lower intensity. This produces a much improved surface appearance and considerably improves the fatigue life over single shot peening. Double shot peening is a patented process, U.S. Pat No. 3,073,022 issued to General Motors. The rights of which are not being enforced. I mention it only to underline the value of the process. The patent papers cover seven pages and include fatigue life charts showing life cycle comparisons between unpeened, single peened, and double peened parts. They leave no dought as to the advantages of double shot peening. Phred
  20. Phred replied to vintageracer's post in a topic in Old Want Ads
    Hey Carl, thanks for the pat on the back. But don't over do it or I'll have to buy a bigger helmet. I have never seen a stock Datsun rod that was shot peened from the factory. Mainly because its so labor intensive. For more info, stay tuned and I'll post a new thread, a short article I wrote that explaines what shot peening is, how its done, etc. But right now, its time for dinner. Stay tuned. Phred
  21. Phred replied to Zrush's post in a topic in Engine & Drivetrain
    I've tested a number of spark plugs on a back to back dyno comparison. I've done the tests on Datsun, Cosworth, and formula ford. None of the gimicky plugs produced more HP. The ones with special alloy electrodes last longer and handle high energy ignitions better. The only time I actually saw a HP difference was when we were able to change from a regular tip to an extended tip plug. This was because the regular gap plug was slightly shrouded. Plugs can have retracted, surface, regular, or extended gaps, or tips. The limitimg factor in the type of tip you can use is the physical clearance between the plug and valve or piston. L series engines without domed pistons will accept projected tip plugs. Also, make sure to use the proper length (3/4") plug. The most effecient plug will start the flame front as far inside the combustion chamber as possible. Finally, always use never-sieze lube on the threads, and torque 12 to15 ft.lbs. Phred
  22. Phred posted a post in a topic in Old For Sale Ads
    This is a 6 month old 4 row re-cored radiator from a 71' 240. I have an invoice for $218.00. The reason I'm selling is because the project is on hold for a while, and when I finish it up, I want to install an aluminum radiator. It weighs about 20 lbs. and will require a stout crate, so the buyer will pay for shipping. Or pick up in Portland, Oregon. Price is firm @ $160.00 Phred
  23. The wheels are the zero offset Z type. As I recall, I couldn't read any difference on the speedo. At the time, every thing else was stock. But I havn't driven it in almost two years now. And next time I do, It will be a Street legal Vintage Racecar. Phred
  24. FWIW, This is what I had into my set. Which fit a 1 1/5" lowered 240 without problems. Local wheel supplier, (4) 16X7 Panasports $876.00 Tire America (4) 225/50ZR16 Comp TA R1 $560.00 " (4) Lifetime Computer spin balance $ 40.00 " (4) stubby chrome valve stems $ 12.00 " (16) Acorn lug nuts $ 16.00 Grand Total $1504.00 Phred
  25. Phred replied to texasz's post in a topic in Suspension & Steering
    MSA shifter pic.

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